Schooner

Schooner

Monday, September 30, 2013

Trial by water

   One of the big tests of any boat, or yacht, is being used. A boat can sit at a dock for years, and years, and once it is taken out, it breaks down, or never starts in the first place. We have had the union pacific out twice this week. The first day we went down river, and got Dana some wheel time. About 45min into the sea trial, i threw a fender overboard. I said to Dana, your husband just fell in. Aside from the 2 min she spent thinking about weather or not she should save him, she was put on the spot as to, what to do. So i instructed her on how to return, and how to stop the boat. she came within 15' of the buoy, and with some coaching  She got within 3' of it. Not bad for a first try. She also learned how to keep a course, under motor. She ridiculed it at first, only to find it a challenge to keep completely straight. By the end of her 90 min she spent piloting the yacht, she was very good at keeping the line fairly straight. Next time she will have to catch the buoy herself.


Tuesday, September 24, 2013

Before the haywire, progress

  So before everything went pear shaped, i did accomplish a bunch of tasks aboard.
First up was the enclosure for the cockpit. It will be chilly as we head south, and this will keep the breeze to a more tolerable level. so i grabbed the uprights from the old camper top of the powerboat, and reused them to see how well they would fit.



i will need to modify the poles a bit, but not too shabby for a first fit.

the second project was increasing floor space in the front bedroom.

before
 during
after

thats it for now.

Friday, September 20, 2013

The loss of a crew member is never easy.

   Tragedy struck our small ship this week with the departure of our son. Midshipman Leonardo has departed our crew to sail with Jesus Christ forever. He will be missed. 

Tuesday, September 3, 2013

hose beware

   Yesterday was inside day. It has been raining for the past two days, so the deck is far to wet to do anything on. I made a list for today.
1. Replace the drive belt on the engine.
2. Turn the water pump on the engine right way round
3. Repair the bow head, and find and inspect the waste water tank

   I thought the first two would take all day and the last, 5 min.
I could not be more wrong. So here is the issue.

   I am very sure this drive belt has over 1000 hours on it. It is worn, stretched, and slipping.
It is being blocked in by the water pump.






   So when it was slipping on the way home i was unable to change it. I am not sure why, but the water pump was installed sideways. not sure what genius did this, but their problem solving skills were poor at best. In the process of changing out the pump direction the black hose with green stripe fell apart in my hand. How fun. I am actually very glad when this happens. I would rather the boat fall apart in my hand, in port, in NY, then have a single failure while at sea.

   So off to the marine store, that didn't have one, then off to napa, to be presented with two options.
Option 1 was a $6 a foot hose option 2 was a $3 a foot hose. I knew this hose would be under suction, so i squeezed both hoses. the $6 hose, even with all my massive hand strength, i could not close it. also when i bent it, it seemed to not kink. so 6' of $6 hose it was. Back to the boat. When i put it back on i replaced the aged SS clamps with brand new USA made ones. This is the hose that come right from the ocean, to the engine. If this had broke when the boat was left alone, it would have sunk the boat.

   Then off came the belt. Back to napa, $16 for the belt, they did not have two.

   I plan to buy a water pump pulley with two belt slots, at a cost of $160. This will allow for a higher power alternator. I will have one built special by my electronics guy with a twin belt pulley on it. No doubt he can build one that delivers 200 amps, VS 90 amps now installed.


   Here is the engine, back together.

   So, onto the next task. I traced the hoses to the center of the hull, by a tank with an inspection cover. So this should be the Black tank right? No. After opening 4 covers, all i could find was fresh waer. That is sort of a good thing, in that our fresh water tank is mostly clean, and very very large. 8'X20'X 12" deep in the center. I emptied out the tank, and in 18 min of filling at 3GPM it was about 1/4 full. i am betting it may be 200 gallons. Also discovered the gauge does not work. I want to put a sight glass on one of the inspection covers, so i can check at any time.
   It is also a bad thing. I have not located the black tank yet. Still 2 more inspection covers. One is marked water., the other is unmarked.





Meanwhile the front head is not connected to the black tank in any way, and the Y valve on the rear head is stuck. What is going on here.....

   I also spent some time DX'ing electrical issues. I believe the wire from the main panel to the depth finder and speed sensor, is shot. i put power to the gauges, and i still have a depth finder! So i will be running a new wire. In fact i am thinking i may buy a 600' spool of 2 conductor marine wire, seems logical.

   More to come, remember to follow me on blogspot!